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ChgrSteve67 Dyno Results

Started by ChgrSteve67, August 04, 2010, 11:29:05 PM

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ChgrSteve67

Got my Charger back from the tuner today.
I took the Fuel Injection off about 10 months ago and have not properly tuned my Charger since I put the Edlebrock carb and MSD dist on.
Since I have a 1,000 mile round trip next weekend I got it over to the tuner.
Here are the results.  Try not to laught too hard. This motor was not built to be 500hp monster.
But let me tell you it sure runs nice and smooth now.

http://i416.photobucket.com/albums/pp248/MPR67/DynoSheets/Dyno1.jpg
http://i416.photobucket.com/albums/pp248/MPR67/DynoSheets/Dyno2.jpg
http://i416.photobucket.com/albums/pp248/MPR67/DynoSheets/Dyno3.jpg
http://i416.photobucket.com/albums/pp248/MPR67/DynoSheets/Dyno4.jpg

Steelshanks

 :cheers:

got her running like a top now eh?

:2thumbs:
Confucius say: "Man who stand on toilet high on pot..."

My 1st Gen Resto Thread

Dans 68

Steve,

The crank hp should be around 325 hp for a "stock '67 383 4-bbl", correct? I'm just a bit perplexed that the driveline losses would be about 26%, especially with the modern 5-speed in there.  :scratchchin:  Good to hear that she is running nice and smooth, though. I'll see you on September 11th.  :cheers:

Dan
1973 SE 400 727  1 of 19,645                                        1968 383 4bbl 4spds  2 of 259

ChgrSteve67

I have looked on the net and people talk about drive train hp loss from 10 to 15% up to 40%.
The only way to really know is to pull the motor and put it on a Engine Dyno (Not going to happen)

The last time I Dyno'ed with a carb it was 242hp with a Holly 700cfm, headers, and the stock 4 speed.
Now its a 650cfm, 5 speed and stock exhaust manifolds.
I'm happy to see the numbers in the same ball park.

Also my Dyno curve is much smoother this time around.
I think the MSD dist and coil really helps the motor consistantly fire on all cylinders.

firefighter3931

Congrats Steve, those are good numbers for a mild 383  :2thumbs:



Ron
68 Charger R/T "Black Pig" Street/Strip bruiser, 70 Charger R/T 440-6bbl Cruiser. Firecore ignition  authorized dealer ; contact me with your needs

ChgrSteve67

Thanks Ron

I forgot to mention that this is on 87 Octane pump gas.

Ghoste

If that 1000 mile round trip is to Columbus, you better hunt me down.

Dans 68

Nah, he's going to "Oregon" http://www.dodgecharger.com/forum/index.php/topic,72254.msg810829.html#msg810829

If any WestCoaster's go to the midwest on a road trip we will definitely talk it up!  :yesnod:

Dan
1973 SE 400 727  1 of 19,645                                        1968 383 4bbl 4spds  2 of 259

Ghoste

Ah, and you know, I should have caught the "round" portion of the trip as I was typing it.

ChgrSteve67

Next year I will be driving Big Red to MI for the CEMA show June 11, 2011 and then to Chicago to pick up the start of Route 66 for the trip Home.

I still have not decided if I will make it to St Louis the days before for the 45th get together yet.

BSB67

Quote from: ChgrSteve67 on August 04, 2010, 11:29:05 PM
Got my Charger back from the tuner today.
I took the Fuel Injection off about 10 months ago and have not properly tuned my Charger since I put the Edlebrock carb and MSD dist on.
Since I have a 1,000 mile round trip next weekend I got it over to the tuner.
Here are the results.  Try not to laught too hard. This motor was not built to be 500hp monster.
But let me tell you it sure runs nice and smooth now.


That is what I would expect from a stockish 383.  The factory numbers were happy.

Did you have fun?  What all did they do in tuning? 

500" NA, Eddy head, pump gas, exhaust manifold with 2 1/2 exhaust with tailpipes
4150 lbs with driver, 3.23 gear, stock converter
11.68 @ 120.2 mph

ChgrSteve67

They timed the motor, Re-curved the distributer, re-jetted the carb and adjusted the choke for cold engine starts.

Since they worked on it for three days I was not around when they ran it on the Dyno.

Not much fun just paying the bill.

I'm very happy with the work they did.